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Krško NPP PSA Update with SG BD System Modifications (CROSBI ID 564132)

Prilog sa skupa u zborniku | stručni rad | međunarodna recenzija

Vrbanić, Ivan ; Bašić, Ivica ; Vuković, Igor Krško NPP PSA Update with SG BD System Modifications // Proceedings and Book of Abstracts of 8th International Conference on Nuclear Option in Countries with Small and Medium Electricity Grids / Pevec, Dubravko ; Subašić, Damir ; Šimić, Zdenko (ur.). Zagreb: Hrvatsko nuklearno društvo, 2010. str. S6-58-1-S6-58-13

Podaci o odgovornosti

Vrbanić, Ivan ; Bašić, Ivica ; Vuković, Igor

engleski

Krško NPP PSA Update with SG BD System Modifications

Evaluations done for the purposes of definition of environmental qualification zones at Krško NPP have shown that, due to potential pipe rupture event in the Steam Generator Blowdown Processing (BD) System, a significant area in the Intermediate Building could become a “harsh” zone. As a consequence, a number of important components, including the Safety Class DC Batteries, Battery Chargers and Motor Driven Auxiliary Feedwater Pumps could be lost following the break in the SG BD line. The same hazard would also affect the Remote Shutdown Panels (Evacuation Panels), located in the affected area, which could result in interactions that would possibly affect safety mitigation systems. The SG BD high energy line break (HELB) would, therefore, represent an initiator with possible significant degradation in plant mitigation capability. Recognizing this, Krško NPP decided to implement a design modification and install the equipment that would detect the SG BD line break and isolate the ruptured pipe in a short time. During plant modification to BD Isolation System the shielding in the form of steel plates for the Cable Trays in the plant room / area IB021 was installed. This was necessary in order to protect the control and power cables for the Remote Shutdown Panels from the dynamic effects produced by a HELB event, such as steam jet impingement, should the postulated break occur in the IB021 area. The results of updated referential Krško NPP PSA model with the above mentioned plant design modifications are presented in this paper. Also the residual risk from the SG BD HELB events, i.e., the risk after the plant modifications are implemented, was assessed. Both Level 1 and Level 2 PSA models were updated in detail. This included the characterization of hazard in the form of hazard damage states, plant response analysis to determine the impact of hazard on the plant equipment in the affected rooms, considering also the containment systems, and Level 1 and Level 2 PSA modelling. The residual risk from the SG BD HELB events was assessed in terms of PSA Level 1 and Level 2.

Krško NPP; safety; PSA; steam generator; blowdown

nije evidentirano

nije evidentirano

nije evidentirano

nije evidentirano

nije evidentirano

nije evidentirano

Podaci o prilogu

S6-58-1-S6-58-13.

2010.

objavljeno

Podaci o matičnoj publikaciji

Proceedings and Book of Abstracts of 8th International Conference on Nuclear Option in Countries with Small and Medium Electricity Grids

Pevec, Dubravko ; Subašić, Damir ; Šimić, Zdenko

Zagreb: Hrvatsko nuklearno društvo

978-953-55224-3-0

Podaci o skupu

8th International Conference on Nuclear Option in Countries with Small and Medium Electricity Grids

poster

16.05.2010-20.05.2010

Dubrovnik, Hrvatska

Povezanost rada

Elektrotehnika